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Caboolture Gliding Club

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 False start Friday

22-May-15

  
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From: Garrett Russell <gjr@powerup.com.au>
Date: Sat, May 23, 2015 at 8:45 AM
Subject: False Start Friday at YCAB
To: cgcmem@mailmanlist.net.au



We had a bit of a false start on Friday which reduced our morning flying, but still managed a total of almost three hours in the air.

The problem was with IKW, grounded by a mechanical glitch revealed in the DI. Duty instructor Bob Turner's eagle eye and ear had found the problem, so while he consulted with Speedy on the ground and with Lindsay on the phone, the rest of us had only GYK and GJY to take out to RWY24.

Only three seats to share between Tony Sorensen, Barry McCarthy, Arthur Mailey, Bob Hainsworth, Charles Hoch, Judith Smith, John Nestor, Kevin Rodda, Jessica Bellamy and myself. Not to mention an AEF passenger to 4,500 feet!

The silver lining was that the conditions which sent us to 24 were also contributing to fairly short flights: strong blustery winds, clear sky, no workable thermals and, for most of the day, no mountain wave. The longest flight time was just 26 minutes, shared by Tony and Arthur on the day’s first launch and Barry with the AEF passenger. The other flights were mostly timed in the teens and there was a constant huddle of members in the sunny lee of the pie cart - the only place we could get away from the biting wind. Not the most enjoyable airfield day.

There was a bright spot when Al Harford generously offered to take one of us in motor glider GHM on a hunt for wave out on the mountains. John Nestor was quickly volunteered as a motor glider virgin and he came back beaming - but also reporting that they could not connect with any wave.

Around the same time Kevin Rodda took off in his own self launcher but came back with a flat battery before being able to start his own wave hunt.

Even the arrival of a knight in shining armour, in the form of Bert Persson to tell us he’d spent the morning inverted in IKW’s cockpit and the glider was now airworthy again, didn’t improve the situation much. The Twin Astir’s two subsequent flights added up to just 35 minutes.

The second of those launches was a tie down flight because by shortly after lunch we all agreed to call it a short day and get out of the wind.

That’s when Bob Turner found 33 minutes worth of lift on the way back to the tie downs in GJY. And Barry McCarthy as pilot in command shared one of the best Blank flights I’ve ever enjoyed - 57 minutes of working wave between 3,000 and 3,500 feet over Caboolture township. We fell just short of the hour, but flight of the day, on a tie down flight, in the lowest performance glider on the field, was a pretty good feeling.

And proof that even a “bad day” at the airfield can end up being “pretty good”.

With special thanks to Dan Kershaw, who filled in at short notice to fly the tug all day, and a get well soon wish to tuggies John Knox and Mike Grady, the days stats:

IKW 2 flights 0:35
GJY 3 flights 1:13
GYK 4 flights 2:04
           
 
Garrett Russell
for the Friday Crew